Back to photostream

Project Gemini MOL (Manned Orbiting Laboratory) / 1965

The Manned Orbiting Laboratory (MOL) was part of the United States Air Force (USAF) human spaceflight program in the 1960s. The project was developed from early USAF concepts of crewed space stations as reconnaissance satellites, and was a successor to the canceled Boeing X-20 Dyna-Soar military reconnaissance space plane. MOL evolved into a single-use laboratory, for which crews would be launched on 30-day missions, and return to Earth using a Gemini B spacecraft derived from NASA's Gemini spacecraft.

 

The MOL program was announced to the public on 10 December 1963 as an inhabited platform to demonstrate the utility of putting people in space for military missions; its reconnaissance satellite mission was a secret black project. Seventeen astronauts were selected for the program. The prime contractor for the spacecraft was McDonnell Aircraft; the laboratory was built by the Douglas Aircraft Company. The Gemini B was externally similar to NASA's Gemini spacecraft, although it underwent several modifications, including the addition of a circular hatch through the heat shield, which allowed passage between the spacecraft and the laboratory. Vandenberg Air Force Base Space Launch Complex 6 (SLC 6) was developed to permit launches into polar orbit.

 

As the 1960s progressed, the MOL competed with the Vietnam War for funds, and resultant budget cuts repeatedly caused postponement of the first operational flight. At the same time, automated systems rapidly improved, narrowing the benefits of a crewed space platform over an automated one. A single uncrewed test flight of the Gemini B spacecraft was conducted on 3 November 1966, but the MOL was canceled in June 1969 without any crewed missions being flown.

 

Seven of the astronauts selected for the MOL program transferred to NASA in August 1969 as NASA Astronaut Group 7, all of whom eventually flew in space on the Space Shuttle between 1981 and 1985. The Titan IIIM rocket developed for the MOL never flew, but its UA1207 solid rocket boosters were used on the Titan IV, and the Space Shuttle Solid Rocket Booster was based on materials, processes and designs developed for them. NASA spacesuits were derived from the MOL ones, MOL's waste management system flew in space on Skylab, and NASA Earth Science used other MOL equipment. SLC 6 was refurbished, but plans to have military Space Shuttle launches from there were abandoned in the wake of the January 1986 Space Shuttle Challenger disaster.

 

 

NASA's Gemini capsule was extensively redesigned for the MOL Manned Orbiting Laboratory program. The resulting Gemini B, although externally similar, was essentially a completely new spacecraft. Gemini B was not designed to fly separately, but rather was launched with the crew aboard attached to the manned orbiting laboratory. After reaching orbit, the crew would shut down the capsules systems and put them into hibernation. They would crawl through an 0.635 m diameter hatch in the heat shield, leading to a tunnel that accessed the MOL itself. After thirty days of operations, the crew would return to the Gemini B, separate from the MOL, and reenter the atmosphere. Gemini B had only 14 hours of free flight time for autonomous operations after separation from the MOL.

 

Several changes were made from the original NASA Gemini, including:

 

-Internal systems were containerized and designed for long term orbital storage

-The cockpit layout was completely redesigned and new instruments were developed

-The cant of the ejection seats were changed in order to make room for the hatch in the heat shield between the crew's shoulders

-Cabin atmosphere was changed to Helium-Oxygen in place of pure oxygen. At launch, the crew breathed pure oxygen in their suits while the cabin was filled with pure helium. During ascent, oxygen from the suits slowly brought the cabin atmosphere up to the helium-oxygen content of the station itself.

-In order to handle higher energy reentries from polar orbit, the heat shield was increased in diameter, so that it actually stuck out a bit from the base of the reentry vehicle.

- The OAMS maneuvering thrusters of the NASA Gemini were deleted; spacecraft orientation in orbit was handled by the forward RCS thrusters.

-The number of solid propellant retrofire motors was increased from four to six. These served double-duty: for deorbit of the Gemini B and as abort rockets for separation of the Gemini from the enormous Titan 3M in case of launch vehicle failure.

 

The prototype Gemini-B, which was launched on a suborbital trajectory, was the refurbished Gemini-2 capsule, making it the first reused spacecraft. It was launched with the MOL-Heatshield Qualification Test on a Titan-3C launch vehicle.

2,626 views
4 faves
1 comment
Uploaded on February 24, 2021
Taken on December 25, 2007